13.1 Installing the cooling unit.
It quickly became apparent that it was impossible to lift the cooling
unit onto the cabinet by hand. Apart from the weight, the cabinet is 1300mm
tall and the bottom of the evaporator has to be lifted over the top. Then
the cooling unit has to be delicately aligned so that the seal and high
side tube is not caught as the unit is lowered.
GE did make a portable hoist specifically for Monitor Top installation
but as this was only used by installers, such an item would be impossible
to obtain now.
For those that want to attempt copying it, this is the GE crane
for the cooling units.
.
An engine hoist is an ideal substitute and is what I used. It is
important that the hoist can be raised at least 2m.
The cooling unit was supported on milk crates which in turn were placed
on the feet of the hoist. Once the hoist was raised, the crates were removed
so the hoist could be pushed in front of the cabinet.
Lowering the top into the cabinet is a tricky procedure and requires
a lot of care. As the high side tube runs right against the cabinet opening,
it is easily damaged. The seal is easily caught on the cooling unit as
it is lowered, so this must be done slowly checking frequently that everything
is in the right position.
As my cabinet was slightly out of square, the top had to be lowered
with the back lip on first and then the cabinet pushed into square as the
front was lowered. Once on, the top lip keeps it square.
The restored CA-2-B15.
14.1 First operation in cabinet.
As always when the cooling unit has not been powered, it is necessary
to run the heater first, to evaporate the Methyl Formate from the oil.
It does not take long for the Methyl Formate to start boiling once the
power applied. This is audible by listening close to the compressor. The
boiling gradually gets louder, and after a few hours it stops. This means
it is ready to be used.
It was found that ice cubes could be frozen in a plastic tray sitting
in the evaporator, so it would appear the temperature was low enough.
14.2 Calibrating the thermostat.
Despite the cabinet temperature appearing to be sufficiently low, the
compressor rarely switched off, even on the No.1 setting. Looking through
the AK service manual (Canadian version of the CK), it appeared that the
thermostat knob might need to be reindexed. The fact that I had removed
the bellows from the rear of the thermostat could have upset calibration.
Also mentioned was the effect of atmospheric pressure on the bellows, and
that at higher altitude the calibration would be different. This was plausible
given the elevation at my location.
My assumption was that given the evaporator temperature should be no
more than 25 degrees F, then that should correspond with the warmest setting;
i.e. 1.
Removing the knob requires the centre disc to be carefully prised out.
I used the smallest size jeweller’s screwdriver I had. With the knob initially
set to 1, I took it off and moved it to 6. Effectively, it had 6 positions
more in the warmer direction. This seemed a good guess with the evaporator
settling at around 25 degrees F. Cycling of the compressor was improved,
but not optimum. This I assumed would be losses through the door seal.
15.1 Door seal.
I was able to purchase a reproduction seal from Don at Rusty Metal
Rescue.
This has to be contact glued into position as it does not have the
barbs that fit the holes around the door edge.
Unfortunately, upon reinstalling the door, I found the bottom left corner
still had a gap. Further investigation revealed the cabinet was slightly
warped in this area. It appears from the dent in the foot below this area
that the cabinet has been dragged with all the force on this leg, thus
applying stress to the bottom of the cabinet immediately above. Given the
impracticality of getting the cabinet perfectly square, I simply added
a thin piece of neoprene seal to fill the gap.
Reproduction foot pads were purchased to replace the originals.
16.1 Non condensable gases again.
Over the course of running the fridge, it had been noticed that after
a few hours performance would drop off, with a low frost line and continuous
running, along with warm cabinet temperature.
Yet, if the fridge was rested for a few days all would be reasonable
again for another few hours.
I had developed a theory that maybe non condensable gases were present
in the compressor walls and the motor and being driven out when warmed
up.
Given that the motor windings would still be likely to contain moisture
(the motor was not heated during evacuation) this seemed a likely scenario.
So, I purged the non condensables again; it took a couple of hours
before the methyl formate appeared.
Purging the non condensables requires oil to be placed in the charge
valve to ascertain positive or negative pressure.
Performance was now excellent. Within a few hours the duty cycle was
perfect; 2-3 mins on and 10-13 mins off. On the No. 9 setting the evaporator
got down to 3 degrees F which was more than sufficient, especially as the
bottom of the cabinet was below freezing.
With this excellent performance still at 11pm, I decided to leave it
on over night. Alas, next morning was a disappointment with the compressor
running continuously, a low frost line, and ice melting off the evaporator.
My theory at this point was that not all the moisture had been driven
out of the motor during the previous purge. Thus it would seem necessary
to repeat purging until it is.
16.2 Float valve blockages.
A further purge was required, but performance was still poor. As non
condensable gases were not the problem, it had to be a blockage. Tapping
on the side of the float chamber’s needle and seat area brought forth a
good flow. Several times the fridge had been run with a gradual decrease
in performance after a day. A pattern was emerging, in that if the fridge
had been rested for a day or more, it would run perfectly but always start
to deteriorate after a day’s running. By this time, power consumption was
under 200W (including transformer and oil heater), and the frost line would
be very low.
With non condensables eliminated as the problem, another theory was
looking plausible. Observing power consumption over the time the fridge
ran correctly showed an initial draw of about 240W. As the fridge cooled
and was cycling normally, consumption went down to about 200-210W.
It would appear that the density of methyl formate decreased as it cooled
because of less strain on the compressor, which in turn relates to less
power consumption. So, with less pressure, there is greater difficulty
in clearing the blockages. This would explain why the blockages largely
cleared themselves on initial power up, but not so after the fridge was
down to normal working temperature.
Running the fridge for 10 days continuously showed up an interesting
pattern. Blockages would usually occur at around 5am which is the coldest
part of the day inside the house. Late at night, the power consumption
would start to drop and the cycle time reduce. With the float seat starting
to block, a higher than normal vacuum would occur in the evaporator which
in turn means the compressor has less vapour to suck in. Thus, the compressor
runs at less of a load. When this happens, the power consumption drops
to about 185-190W. After this, the frost level falls because the
incoming liquid is not being replenished as fast as it is being evaporated.
Short cycling then starts to occur. This is presumably because with less
frost on the evaporator, it is less able to store the cold temperature.
Eventually, the frost line drops so that it is no longer near the thermostat
bulb, and the compressor runs continuously.
16.3. Compressor timer.
Not always being at home meant that in the event of the compressor
running continuously, I would not be able to turn it off and/or clear the
blockage. So, I built up a timing circuit that sensed when the compressor
was running. If the compressor ran for more than 25 minutes (or any other
desired time), power would shut off and remain so until manually reset.
This would protect the motor from an excessive run time. Importantly, it
meant I could leave the fridge running unattended and not worry about it.
Operation is sensed by a current transformer. This actuates an Omron H3CR
timer set for 25 minutes.
If the timer is not reset within that time, a relay latches cutting
power to the fridge.The relay remains latched while ever the 120V supply
is present.
16.4 Improvement in operation.
Running the fridge for several months did improve things considerably.
The blockages became much less frequent. In fact, instead of hours apart,
it was now days. It would appear that whatever was causing the valve to
stick may have been gradually dissolved. Alternatively, the constant flow
of methyl formate and valve operation may have “machined” the needle and
seat for a less sticky fit. There is no difficulty in freezing ice in plastic
trays and the cycling times are good; 2-3 minutes on and at least 10 minutes
off. Correct temperature is with the control in position “3”. This suggests
the calibration is satisfactory, although for correctness the knob should
be moved to “5” before screwing back in.
17. Shelves.
Only two of the three shelves were present. They are made of steel
and either galvanised or zinc plated. The finish is too dull to be nickel
or chrome. A previous owner has painted over this with white enamel.
The shelves had been painted in white enamel over the original plating.
The black objects on the lower shelf are the original foot pads.
I had the shelves replated by Artarmon Electroplating. It appears that they were originally zinc plated and this is what was recommended. Nickel or chrome was advised against due to rusting in the moist environment.
Like new again, the shelves were the final part of the restoration.
18. Acknowledgements.
This was my first entry into the world of refrigeration and would have
found it considerably more difficult without the help of others. There
is a lot of negativity about working on Monitor Tops around the internet,
and when I found the Flickr group all that changed. In particular, due
acknowledgements must be given to the following group members for their
help:
19. Suppliers.
Monitor Top Refrigerator Forum (replacement for Yahoo and Flickr Groups).
Yahoo group - GE Monitor Top Fridges. (no longer active due to Yahoo changes).
Flickr group - Monitor Top Refrigerators.
Postscript.
Unfortunately, the reliability of the float valve in this machine turned
out to be very problematic. It would block up frequently. After the success
of the CA-1, the obvious solution was to do a capillary conversion.
See the details here.
This improved reliability considerably, but evidently the system had
been badly contaminated because NCG build up was still frequent, requiring
purging every month. The decision was made to confirm this was not due
to leakage, so the unit was evacuated and filled with 50psi of R22. A leak
detector could not find any evidence of leakage. Much to my surprise, the
R22 must have had some kind of cleaning effect, because after evacuation
of the R22 and refilling with methyl formate again, performance was really
good. No purging was required for seven months. Cycling times were good;
4.5 mins run and up to 16 mins off with a cabinet temperature of about
34F.
In January 2015, a year after doing the capillary tube conversion,
a high side blockage occurred. The inline strainer was completely clean
which was good news - no more corrosion evident. However, it indicates
the problem of the blocked evaporator remains. Again, I am led to believe
this cooling unit has been left open to the atmosphere for quite a long
time.
A replacement evaporator was subsequently installed. A check with nitrogen
flow showed that the original was still partially blocked. A couple of
years of methyl formate flowing through it had not dissolved the blockage
as I had hoped. Since the new evaporator was installed, performance has
been completely reliable. This is now my main fridge.